Preliminary technical conclusions of the BP Oil Spill Commission
Published: November 8, 2010, 12:00 am
Updated: March 27, 2011, 2:04 pm
This article has been reviewed by the following Topic Editor:
Cutler J. ClevelandEditor's note: This is a verbatim reproduction of matetrial posted by the National Commission on the BP Deepwater Horizon Oil Spill and Offshore Drilling during Meeting 5, November 8-9, 2010, Washington D.C. The Commission's purpose is to examine the facts and circumstances to determine the cause of the Deepwater Horizon Oil Disaster.
Prelimary Conclusions-Technical
- Flow path was exclusively through shoe track and up through casing.
- Cement (potentially contaminated or displaced by other materials) in shoe track and in some portion of annular space failed to isolate hydrocarbons.
- Pre-job laboratory data should have prompted redesign of cement slurry.
- Cement evaluation tools might have identified cementing failure, but most operators would not have run tools at that time. They would have relied on the negative pressure test.
- Negative pressure test repeatedly showed that primary cement job had not isolated hydrocarbons.
- Despite those results, BP and TO personnel treated negative pressure test as a complete success.
- BP’s temporary abandonment procedures introduced additional risk.
- Number of simultaneous activities and nature of flow monitoring equipment made kick detection more difficult during riser displacement.
- Nevertheless, kick indications were clear enough that if observed would have allowed the rig crew to have responded earlier.
- Once the rig crew recognized the influx, there were several options that might have prevented or delayed the explosion and/or shut in the well.
- Diverting overboard might have prevented or delayed the explosion. Triggering the EDS prior to the explosion might have shut in the well and limited the impact of any explosion and/or the blowout.
- Technical conclusions regarding BOP should await results of forensic BOP examination and testing.
- No evidence at this time to suggest that there was a conscious decision to sacrifice safety concerns to save money.
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Citation
National Commission on the BP Deepwater Horizon Oil Spill and Offshore Drilling (Content Source);Cutler J. Cleveland (Topic Editor) "Preliminary technical conclusions of the BP Oil Spill Commission". In: Encyclopedia of Earth. Eds. Cutler J. Cleveland (Washington, D.C.: Environmental Information Coalition, National Council for Science and the Environment). [First published in the Encyclopedia of Earth November 8, 2010; Last revised Date March 27, 2011; Retrieved May 19, 2013 <http://www.eoearth.org/article/Preliminary_technical_conclusions_of_the_BP_Oil_Spill_Commission>
Editor's note: This is a verbatim reproduction of matetrial posted by the National Commission on the BP Deepwater Horizon Oil Spill and Offshore Drilling during Meeting 5, November 8-9, 2010, Washington D.C. The Commission's purpose is to examine the facts and circumstances to determine the cause of the Deepwater Horizon Oil Disaster.
Prelimary Conclusions-Technical
- Flow path was exclusively through shoe track and up through casing.
- Cement (potentially contaminated or displaced by other materials) in shoe track and in some portion of annular space failed to isolate hydrocarbons.
- Pre-job laboratory data should have prompted redesign of cement slurry.
- Cement evaluation tools might have identified cementing failure, but most operators would not have run tools at that time. They would have relied on the negative pressure test.
- Negative pressure test repeatedly showed that primary cement job had not isolated hydrocarbons.
- Despite those results, BP and TO personnel treated negative pressure test as a complete success.
- BP’s temporary abandonment procedures introduced additional risk.
- Number of simultaneous activities and nature of flow monitoring equipment made kick detection more difficult during riser displacement.
- Nevertheless, kick indications were clear enough that if observed would have allowed the rig crew to have responded earlier.
- Once the rig crew recognized the influx, there were several options that might have prevented or delayed the explosion and/or shut in the well.
- Diverting overboard might have prevented or delayed the explosion. Triggering the EDS prior to the explosion might have shut in the well and limited the impact of any explosion and/or the blowout.
- Technical conclusions regarding BOP should await results of forensic BOP examination and testing.
- No evidence at this time to suggest that there was a conscious decision to sacrifice safety concerns to save money.
Are you absolutely sure you want to delete this article? This process cannot be undone and is permanent.
Yes, Delete This Article
Are you absolutely sure you want to remove this article? This process cannot be undone and is permanent.
Yes, Remove This Article
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